A bit of an engine problem and some adjustments
 
The engine started all right and it was fun. |
In the end the engine had to be removed and checked for dirt in the oil passages. |
As the engine is out, the cut out for the rag joint at the steering box was enlarged, as it became apparent that it was too small. |
After some searching I found a pair of connecting rods with suitable diameter big ends to make a column drop from. These are early sixties Simca Aronde items. |
A few days later, this is what the connecting rods look like in their new surroundings. |
October 24:th
The Essex has been test driven, and successfully too!
Just a few hundred meters, but without head lights in the dark...
Maybe a real shake down test can be performed some day soon.
October 25:th
Here's a small movie clip showing the start of a shake down test which
amounted to a little less than 3 miles.
The Essex performed very nicely, and the most notable shortcoming is the too high seating
position, which will be corrected when fabricating the front bench.
The Essex is back in the garage after a couple of short shake down tests. |
An exhaust system is next on the agenda. The temporary electrical system with the ignition coil taped to the brake master cylinder also seen here. |
Here's the finished, though unpainted exhaust manifold. The right hand one looks similar, but is a little less curvy as it doesn't have to work its way around the steering shaft (arrow). |
The twin exhaust with polished stainless |
Go on to part twelve
[ Other project cars ]
[ Outside the shop ] [ 2 ] [ 3 ] |
[ Introduction ]
[ Part1 ]
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